首页 | 本学科首页   官方微博 | 高级检索  
     

巷道复杂岩层中钻孔原位注浆试验
引用本文:黄华元, 刘振兴, 范成洲, 秋实, 刘俊鹏. 巷道复杂岩层中钻孔原位注浆试验[J]. 煤田地质与勘探, 2013, 41(1): 67-71. DOI: 10.3969/j.issn.1001-1986.2013.01.014
作者姓名:黄华元  刘振兴  范成洲  秋实  刘俊鹏
作者单位:1.西北核技术研究所, 陕西 西安 710024
摘    要:针对大漏失地层,探索增强某巷道复杂岩层抗渗性的技术途径,采用钻孔原位注浆方法开展了注浆试验研究。钻孔采取两步法注浆工艺,大漏失地层和一般漏失地层一次注浆的堵水效率一般可达80%以上,部分可达100%,微漏失地层的堵水效率可达100%。但有一些大漏钻孔采用现有注浆方法不能有效封堵,应进一步研究其他注浆措施,并需研究对注浆孔口及周边表面的快捷有效的封堵技术。

关 键 词:巷道  复杂岩层  原位  压水  注浆试验
收稿时间:2012-05-09

Experimental research on in-situ grouting through holes in complex rock stratum in tunnel
HUANG Huayuan, LIU Zhenxing, FAN Chengzhou, QIU Shi, LIU Junpeng. Experimental research on in-situ grouting through holes in complex rock stratum in tunnel[J]. COAL GEOLOGY & EXPLORATION, 2013, 41(1): 67-71. DOI: 10.3969/j.issn.1001-1986.2013.01.014
Authors:HUANG Huayuan  LIU Zhenxing  FAN Chengzhou  QIU Shi  LIU Junpeng
Affiliation:1.Northwest Institute of Nuclear Technology, Xi'an 710024, China
Abstract:Aiming at the search of impervious technique in an engineering tunnel, in-situ grouting by boreholes was adopted for grouting experimental research. The researches indicate that most rock strata in this area leak severely. By assuming the technology of two-step grouting, pounding ratios in most rock strata with severe leakage achieved up to 80% and in some area to 100%. But some boreholes need further investigations on grouting measures for improving pounding ratios effectively. 
Keywords:tunnel  complex rock stratum  in-situ  water pressing  grouting experiment
本文献已被 万方数据 等数据库收录!
点击此处可从《煤田地质与勘探》浏览原始摘要信息
点击此处可从《煤田地质与勘探》下载全文
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司  京ICP备09084417号