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水力吹填地基的水平排水板振动碾压处理法
引用本文:何开胜,沈珠江,张广旗,黄保东.水力吹填地基的水平排水板振动碾压处理法[J].岩土力学,2001,22(1):109-113.
作者姓名:何开胜  沈珠江  张广旗  黄保东
作者单位:1. 南京水利科学院土工研究所,
2. 中国水利水电工程总公司,
摘    要:对水力吹填地基,本文提出了在吹填过程中分层铺设水平向排水板并振动碾压的处理方法和应用实例,处理后的标准贯入试验显示吹填细砂的标贯击数提高到不处理时的3-4倍,标准贯入,静力触探和荷载板试验表明,处理后的吹填细砂达到了电厂地坪要求的承载力,沉降和不液化目标,取得了显著的经济和社会效益。

关 键 词:水力吹填  水平排水板  振动碾压  地基处理  标贯击数  吹填细砂  预压法
文章编号:1000-7598-(2001)01-0109-05
修稿时间:2000年9月22日

Dredged fill treatment using horizontal wick drains combined with vibrating roller compaction
HE Kaisheng,SHEN Zhujiang,ZHANG Guangqi,HUANG Baodong.Dredged fill treatment using horizontal wick drains combined with vibrating roller compaction[J].Rock and Soil Mechanics,2001,22(1):109-113.
Authors:HE Kaisheng  SHEN Zhujiang  ZHANG Guangqi  HUANG Baodong
Abstract: This case history described the improvement of saturated fine grained hydraulic fill using horizontal wick drains combined with vibrating roller compaction. The site is situated on the north shore of the Meghna River,Bangladesh,in an area underlain by thick siltyfine sand. Horizontal wick drains is placed within the fine sand fill during construction as the fill is placed the fill having horizontal wick drains is compacted in layers by vibrating roller. After treatment SPTs,CPTs and loading plate tests were carried out,indicating that SPT N-values increase 3∽4 times compared to the non-treated fill and employer's requirements on bearing capacity of dredged fill,post-settlement and anti-liquefaction are achieved. Thus,3 200 000 USD were economized in the costs of ground treatment compared to the stone column method in tender.
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