首页 | 本学科首页   官方微博 | 高级检索  
     

低能量强夯法加固粉质黏土地基试验研究
引用本文:周健,史旦达,贾敏才,崔积弘. 低能量强夯法加固粉质黏土地基试验研究[J]. 岩土力学, 2007, 28(11): 2359-2364
作者姓名:周健  史旦达  贾敏才  崔积弘
作者单位:1.同济大学 地下建筑与工程系,上海 200092;2.上海海事大学 交通运输学院,上海 200135; 3.同济大学 岩土及地下工程教育部重点实验室,上海 200092
基金项目:上海市重点学科建设项目
摘    要:结合上海某铁路集装箱中心站地基处理工程,针对其场区上部粉质黏土、下部砂质粉土的地基条件,对低能量强夯法加固此类地基的适用性进行了现场试验研究。通过对夯击过程中超静孔隙水压力随夯击次数、深度、距离的变化规律及在不同性质土层中的增长与消散规律的研究,提出了运用试验手段确定强夯夯击次数、夯点间距、有效加固深度及两遍强夯间隔时间等施工参数的方法。同时,用静力触探试验和标准贯入试验对地基加固的效果进行了检验,结果说明低能量强夯法加固粉质黏土地基的适用性,从而进一步拓宽了低能量强夯法的应用范围。

关 键 词:低能量强夯  真空井点降水  超静孔隙水压力  地基处理  
文章编号:1000-7598-(2007)11-2359-06
收稿时间:2005-11-29
修稿时间:2005-11-29

In-situ test study on low-energy dynamic consolidation method to improve a silty clay ground
ZHOU Jian,SHI Dan-da,JIA Min-cai,CUI Ji-hong. In-situ test study on low-energy dynamic consolidation method to improve a silty clay ground[J]. Rock and Soil Mechanics, 2007, 28(11): 2359-2364
Authors:ZHOU Jian  SHI Dan-da  JIA Min-cai  CUI Ji-hong
Affiliation:1. Department of Geotechnical Engineering, Tongji University, Shanghai 200092, China; 2. Department of Communications and Transportation, Shanghai Maritime University, Shanghai 200135, China; 3. Key Laboratory of Geotechnical and Underground Engineering of Ministry of Education, Tongji University, Shanghai 200092, China
Abstract:Based on a major construction project in Shanghai of which the ground consists of a silty clay layer in surface and underlying a sandy silt layer,in-situ test study on the fitness of low-energy dynamic consolidation method(LEDCM) is done.By analyzing the variation of excess pore water pressure with depth,distance and the impact number,and considering the increasing and dissipation regularity of excess pore water pressure in different soil layers,a method to choose the construction parameters of LEDCM such as the optimal impact number,the appropriate impact space,the effective strengthened depth and the reasonable interval between two impact passes,by experimental means is proposed.At the same time,the field detective trials including the static cone penetration tests and the standard penetration tests are given to evaluate the effectiveness of improvement,and the results indicate the validity of LEDCM to treat the silty clay ground and also further broaden the application range of LEDCM.
Keywords:low-energy dynamic consolidation  vacuum well dewatering  excess pore water pressure  ground improvement
本文献已被 CNKI 维普 万方数据 等数据库收录!
点击此处可从《岩土力学》浏览原始摘要信息
点击此处可从《岩土力学》下载全文
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司  京ICP备09084417号